节点文献

龙背湾低导流洞进口边坡变形稳定分析及加固处理

Analysis of deformation stability on Longbeiwan low diversion tunnel entrance slope and reinforcement

  • 推荐 CAJ下载
  • PDF下载
  • 不支持迅雷等下载工具,请取消加速工具后下载。

【作者】 李毅陈益峰周嵩周创兵

【Author】 LI Yi1,2,CHEN Yifeng1,2,ZHOU Song1,2,ZHOU Chuangbing1,2(1.State Key Laboratory of Water Resources and Hydropower Engineering Science,Wuhan University,Wuhan 430072,China;2.Key Laboratory of Rock Mechanics in Hydraulic Structural Engineering,Ministry of Education,Wuhan University,Wuhan 430072,China)

【机构】 武汉大学水资源与水电工程国家重点实验室武汉大学水工岩石力学教育部重点实验室

【摘要】 利用勘测的龙背湾水电站低导流洞进口边坡表层岩体参数,分析自然边坡的安全状态,修正边坡表层岩体的强度参数,并进行初始应力场计算。采用多节理本构模型,对边坡开挖时出现的卸荷裂缝处的岩体进行模拟,并分析裂缝的成因。对初步的加固措施进行模拟,分析开挖过程中,边坡的变形、稳定情况,并在此基础上,对原加固方案进行修改和补充,结合边坡的水位骤降工况,分析边坡的变形稳定情况。研究结果表明:加固措施具有可行性和有效性,为边坡的开挖、加固提供了理论依据。

【Abstract】 Using the investigated rock parameters of Longbeiwan low diversion tunnel entrance slope,the status quo of the slope was analyzed.The rock strength parameters of the slope surface were modified and the initial stress field was calculated.Multi-joint model was used to simulate the unloading cracks during the excavation,and the causes were analyzed.The original reinforcement measures were simulated,and then,the deformation and stability situation during the excavation were analyzed.On the basis of these,reinforcement measures were modified and enhanced,and deformation and stability were analyzed when the slope is being suffered by a rapid drawdown of water level.The results show that the reinforcement measures are feasible and effective,which can provide theoretical support to the excavation and reinforcement of the slope.

【基金】 国家自然科学基金资助项目(51079107,51179136);国家优秀青年科学基金项目(51222903)
  • 【文献出处】 中南大学学报(自然科学版) ,Journal of Central South University(Science and Technology) , 编辑部邮箱 ,2013年07期
  • 【分类号】TV223
  • 【下载频次】139
节点文献中: 

本文链接的文献网络图示:

本文的引文网络