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催化汽油加氢脱硫装置运行技术分析
The Technical Analysis of FCC Gasoline Hydrodesulfurization Unit Operation
【摘要】 中海油惠州炼化分公司新建一套50万吨/年全馏分催化汽油加氢脱硫装置(CDOSFRCN),以满足公司汽油升级至国Ⅳ、Ⅴ标准的要求。装置运行表明,惠炼催化汽油经CDOS-FRCN处理后,汽油产品硫含量降至50 ppm和10 ppm时,RON损失分别为0.2和1.4。CDOS-FRCN技术具有流程简单、投资省、能耗低的特点,可为炼油厂汽油质量升级提供经济适用、脱硫灵活的技术方案。
【Abstract】 CNOOC Huizhou Refining & Petrochemical Company newly built a set of 500 kt/a full cut FCC gasoline hydrodesulfurization unit(CDOS-FRCN) in order to meet the needs of enhancing the company’s gasoline standard to National Ⅳ Standard and National ⅤStandard. The operation of the unit indicates that, after the treatment of CDOS-FRCN, when gasoline product sulfur content reduces to 50 ppm and 10 ppm, Huizhou Refi ning & Petrochemical Company’s FCC gasoline RON loss is respectively 0.2 and 1.4. CDOS-FRCN technology has the characteristics such as simple process, economical investment and low energy consumption and can provide a economical and fl exible desulfurization technical scheme for refi neries to upgrade gasoline quality.
【Key words】 FCC gasoline; full cut; hydrodesulfurization; catalyst; RON; CDOS-FRCN technology;
- 【文献出处】 当代石油石化 ,Petroleum & Petrochemical Today , 编辑部邮箱 ,2013年09期
- 【分类号】TE96
- 【被引频次】4
- 【下载频次】46